The Bachmann Shay is an excellent engine that has been very well received. It runs very smoothly, pulls as well as any Large Scale engine and is very well detailed. Further, it is 1:20.3 scale which is correct for the 3' gauge of the prototype.
However, there is always something that can be improved on any engine. The Shay is no exception. This page documents some of the little things about the Shay that I have discovered that might be of use to other Large Scalers.
The video tape that comes with the engine has detailed instructions about lubricating the engine. However, it doesn't tell you everything.
The Shay comes with a jewelers screwdriver to take out the screws on the bottoms of the trucks. This screwdriver is totally inadequate for the job. Some Chinese assembler used a MUCH bigger screwdriver to install the screws and getting them out the first time can be a challenge.
Get a REALLY GOOD #1 Phillips head screwdriver to start with. Then work a finger around the back of the truck behind the screw that you are working on to support the truck and use all the force you can muster to press the screwdriver into the screw head before trying to dislodge it. I've done 2 Shays and each of the 32 screws was a challenge to get loose, but I didn't mess up any of them. When you reinsert them, do not tighten them past snug.
Get rid of the white grease that Bachmann uses and replace it with a high quality gear grease such as LGB 51020 gear grease.
The Shay is a big engine. Even though the prototype was a fairly small locomotive, due to its scale it is taller and wider than most other Large Scale engines. This can cause problems on layouts that have tight clearances, like mine for instance.
The Shay will run on 2' radius track and doesn't look too bad doing it. Shay's were designed to run on twisting track so they are at home on tight curves. However, the Bachmann Shay is intolerant of poorly leveled track and will derail each and every time on bad track. If you experience derailment problems at particular parts of your railroad, get a small level and check the track every 6" or so through that area. If the track is out of level by more than half a bubble, fix it.
The Shay is 5" wide over the widest protrusions and 21" long over the end steps. On 2' radius curves the engine overhangs 4-1/8" from the track centerline on the inside and 3-3/4" on the outside. With the standard stack, the engine stands 7-7/8" from the railhead. With the modified stack shown in the lead photo, the tallest point is the whistle which is 7" above the railhead.
The modified stack came from a defunct R/C Big Hauler. It required a little filing to make it fit, but it looks and works fine. There are also after market metal oil stacks now available that are designed to accept an LGB smoke unit.
If the whistle is still too tall for you, as it was for me, then it is fairly easy to fix. I pulled the handrail standoffs, whistle and pops from the steam dome and then pulled off the dome. I then cut a 1/4" section out of the middle of the dome above the holes for the handrail standoffs and then glued it back together. I filed it to fit, painted it to match (Engine Black) and then put it back in place and reinstalled the standoffs, whistle and pops.
There are other clearance problems with the Shay. The brake beams hang very low and WILL hang up on LGB screw clamp track connectors. The brake beams and end steps will barely clear LGB and Aristo turnout motors.
The cab is so wide that it will only clear the lamp stands on LGB 1056 uncoupling tracks when the lamp is rotated parallel to the track.[ Top ]
The Shay is equipped with flickering ashpan and firebox lights. These are simulated with LEDs. The red and yellow ones both flicker, the red ones stay on about 2/3 of the time and the yellow ones 1/3 of the time. The effect is pretty good while it is going, but the engine has to be moving fairly fast, way faster than the prototypical maximum 10-12 mph, before the flickering will start. The speed that the flickering starts is somewhat dependent on your power pack. If you use pure DC, you might not see them start flickering at all. They work a little better with Aristo PWC power, but still not real well.
My thanks to Garry Paine for taking the time to trace out the circuit. The top part consists of an adjustable regulator set to 9 volts and a cab light control circuit. The bottom part of the circuit is the multivibrator which flickers the LEDs. It will light the red LEDs at lower than 9 volts on the internal regulated bus, but does not start to flicker until a full 9 volts is reached. Due to the overhead of the LM317 regulator and the bridge rectifier, about 12 volts is needed on the track to get the circuit going. At 12 volts, the Shay is really trucking so its hard to see the lights anyway. If you run at anything like prototypical speeds, you'll never get going that fast.
I added a 50 micro farad capacitor to the output of the bridge rectifier that will charge off any peaks of power that might be applied to the track so that the regulator has the best chance of working at lower average input voltage. Since I use an Aristo Train Engineer which puts out full voltage pulses even at very low speed, the addition of this capacitor causes the cab light, headlights and the flickering lights to come full on just as the engine starts to move. With pure DC power there will be no noticeable improvement.
The downside of this change is that the cab light starts to flicker heavily. The cab light is driven by a circuit that will shut off the cab light when the input voltage to the regulator IC gets too high. I personally don't seen the advantage of this "feature" so I disabled it by cutting a lead on the 1.8K resistor (labeled R9 on the circuit board). This turns on the cab light control transistor all the time.
After this change, I found that the cab light was too bright, it shines as bright as the headlight. I added 100 ohms in series with the cab light to tone it down. If you want to reduce the intensity of the cab light, unsolder one of the wires labeled L1 and add a 100 ohm resistor in series with the wire.
If you decide to do any other wiring on the flicker board, locating the wires can be somewhat of a pain. The following photo shows what function each wire pair provides. This photo is of a 1st run Ely Thomas #5 Shay, newer models may or may not be the same.
The Shay contains a standard Bachmann smoke unit, which means that it'll burn up in a short second if you let it run dry. This is a problem as you can't put more than a few drops in the smoke generator and it smokes so strongly that the smoke fluid runs out in a couple of minutes.
If the smoker works, but smokes weakly, it may be possible to improve the smoke output at zero cost, see my Smoke Tips page for details. The downside is that it may go through smoke fluid faster and be even more likely to burn up if it runs dry.
One of mine burned up so I changed it out with an LGB unit which works much better. It doesn't generate as much smoke but it generates enough and it'll run for 15 minutes or more.
Gary Cook sent me some instructions as to how he changed out his, thanks Gary. Here's my slant on the modification after doing one myself.
The plan is to use an LGB 5 volt replacement smoke element and a common 5 volt regulator circuit. All this stuff can be mounted in the location of the existing smoke element.
The capacitor is optional. If you use pure DC track power, it won't have any effect. The track voltage will have to be above about 8 volts before the smoke generator will start to work well. Unfortunately, at 8 volts, the Shay is moving right along. If you use Aristo PWC, the capacitor will charge to the peaks (18 to 22 volts depending on the input voltage to your TE receiver) and the regulator will have enough average input voltage to work as soon as the Shay gets moving at all. You'll get full intensity smoke at almost any speed.
LGB smoke units like about 10 to 15 drops of smoke fluid. Less means less smoke duration. More will prevent the smoke unit from getting hot enough to smoke well, it'll just sputter.
The Shay is delivered to accept a sound system. There is a chuff switch in the engine assembly that closes 3 times per crank turn (half the prototypical rate). This switch is brought back to the tender for easy access on a pair of yellow wires. In the tender there is also a small printed circuit board with a bridge rectifier on it that supplies constant polarity power a sound system. This board is nearly useless and is usually scrapped during sound system installation. There is also a pocket for mounting a speaker.
There are four sound systems available now for the Shay. They are available from Phoenix, PH, Sierra and Soundtraxx.
There have been some complaints about the small battery in the PH unit but there is an accessory charger available as described on the RS-3 Tips page. I have also seen some notes that users of Aristo PWC are not experiencing the battery discharge problem with the Shay and the PH sound system. This is probably because the sound system is accepting adequate charge from the PWC pulses even at very low average speeds. The PH system in my RS-3 charges at the first hint of PWC track voltage with the accessory charger installed. The design of the RS-3 system is a little different such that the Shay system should charge from PWC properly without the accessory battery charger. Without PWC, the charger can be set up to charge the battery offline without running the engine.
After I got my Shays, I didn't want to wait for a custom sound system to be released, and because I am fundamentally cheap, I literally hacked the sound board out an old R/C Big Hauler and installed it into the tender. Since I retained the 9 volt battery, I had only to hook the old sound board up to the yellow wires and install the speaker from the old Big Hauler in the tender floor. I also installed a shutoff switch under the water hatch. I used one of the old slide switches from the R/C Big Hauler. This sound system isn't the greatest in the world, but it is better than stealth mode. See Better Bachmann Sound for more information about using and improving the Bachmann sound system.
There is one important thing to note about the chuff switch which will affect any of the sound systems. The switch is mounted behind the engine assembly and runs off the piston rods. The rods are driven from the crank which is in turn driven by only the front truck. The shaft to the rear truck freewheels. When you slip off the square shaft to the front truck to lubricate it, there is a 50% chance that you'll get it back on 90 degrees off the orientation that it was before you removed the shaft. You'll know that you got it wrong if the engine chuff rate becomes unsteady when the front truck is in a tight right turn. A universal joint provides uneven rotational speed transfer when it is off axis. If the two joints on the front shaft are oriented correctly with respect to each other, these speed transfer errors will cancel. If it is wrong, they will add. This will result in uneven crank speed and therefore uneven chuff switch closures. If you hear uneven chuffs, simply pull out the front shaft, rotate it 90 degrees and reinsert it.[ Top ]
"Chili" John Pritchard offers these instructions for installing a Kadee 821 on the Shay.
The Kadee 821 couplers can be easily installed on the Shay. The shallow depth of the box makes them ideal for use in the existing coupler pockets. But first, the end beams have to be modified and the coupler boxes lowered so that the couplers end up at the right height.
Truck mounting couplers is
easy. For the LGB Knuckle, just remove the stock coupler and
install the LGB Knuckle. It will look ugly as sin but it will also
work fine on 2' radius curves.
For the Kadee coupler, remove the original coupler, cut off the end of the coupler mounting tang and screw on a Kadee #831 using the original screw and the original hole. Mounting the coupler this way leaves a lot to be desired from a visual viewpoint, but it will work fine on 2' radius curves.
Dave Goodson has offered these instructions for modifying the valve gear so that it will shift itself from forward to reverse depending on the direction of motion of the engine. Dave supplied the instructions, I supplied the pictures that I took when I did this modification myself following his instructions.
Dave Goodson writes:
To modify your Bachmann Shay to have functional reverse linkage that "floats" in and out with direction, proceed as follows:
Remove engine from locomotive. This is accomplished by removing the lower firebox cover (2 screws), disconnecting drive shafts, and removing two Phillips head screws between the cylinders. Rotate two "lugs" inside firebox until they align with the slots, and carefully work the engine away from the chassis. Pull pin connected to link shaft arm out of cab floor.
Next, remove the pin that went into the cab floor from the shaft completely. It will not be reused. (editor's note) There doesn't seem to be an easy way to remove this pin so I just cut it off.
Work the linkage "in" and "out" many times, oiling the moving parts carefully. Look for any binds and try to remove them.
Set the engine back into position on the chassis. Push the links in, and slowly rotate the crankshaft by hand. You will see that the horizontal links will hit the top of the "I" beam of the frame in three places.
You need to grind the flange of the frame off at these three points (be liberal fore-and-aft) until nothing sticks out past the center vertical leg of the frame. I like to bevel the top slightly. Touch up the ground areas with engine black. Reinstall the engine with the two screws through the cylinders only at this time.
(editor's note) When you do the grinding, shield the engine assembly and the trucks with paper towels so that the metal shavings do not stick to the oil that's probably all over the exposed moving parts. When this picture was taken, I had vacuumed up all the big pieces. It took wiping with a cotton swap to pick up all the little stuff.
There are many production variations of clearance between the arm on the rear of the reverse shaft (that you pulled the pin from) and the cab support right next to it. On my unit (early), to clear the support, I only had to bend the arm slightly forward. Worse case on some is the arm must be removed from the shaft or the cab support must be trimmed or removed. Make sure the links move freely in and out with no interference to the support.
Once this is done, finish the installation by twisting the dogs of the lug 90 degrees, reinstall the firebox cover.
You may not get smooth engagement at first, and you may need to oil frequently for the first week or so, but the links should shift fully in about one actual foot of track movement. Visitors may not notice this at first, but you can point it out to them, and YOU know it works!
The Old Curmudgeon
Most Shays tend to make an annoying tap-tap sound as the engine runs. After a year and a half of listening to it and making marginally effective stabs at making it go away, I've at least figured out exactly what is happening.
The tapping is caused by an interaction between the connecting rod, the crosshead and the sound switch. When the piston rod pushes all the way up into a cylinder, it contacts a leaf switch which is used to trigger a chuff from a sound system. The pressure caused by the switch is slight, but it is enough to cause the crosshead to cock slightly in the crosshead guides. The direction that it cocks is determined by the angle of the connecting rod working against the crankpin. As the connecting rod moves over top dead center, its angle changes to the other direction, and the crosshead snaps to the other crosshead guide causing an audible tap.
I found that covering the crosshead guide with heavy gear grease damps the movement of the crosshead and tends to prevent the tap sound. Since it is very difficult to get to both crosshead guides even with a grease bearing toothpick, this operation is more easily performed with the engine assembly removed from the locomotive. You can follow the directions in the section above for removing the engine. You also need to unsolder the two wires going to the sound switch and solder them back on when you reinstall the engine assembly.
A permanent fix for this problem is to entirely remove the sound switch assembly. The whole contact assembly comes off the back of the engine assembly with three screws. Your sound system will then need to use another method to set the chuff rate, perhaps by voltage controlled chuffing or with another sound contact switch installed somewhere else.
The Shay comes with an assortment of tools and accessories that can be hung or placed anywhere a real tool might be found.
After some considerable discussion on the LSOL Workshop,
Rick Henderson offers that the item in the lower left is a clamp to
hold down the two re-railers. It seems plausible.
Silver Ridge Mining Co. in Mesa AZ (602-854-0418) makes a cast resin oil bunker ($23 +$2 shipping) for the Shay for those of you who would like to convert your Shay to oil. This casting is highly detailed and takes about 2 minutes flat to install. Coal and wood burners produced a lot of cinders and tended to start fires. This was a special problem for loggers. Many logging Shays were converted to burn oil to reduce the burning cinder problem. In many locations, oil was easier to obtain than coal and didn't require much in the way of fueling equipment except a tank truck and a pump.
Daniel Daugherty writes: You should mention the Hillside Railways Flickering Firebox kit for the B-Shay. $99.00 replaces the complete wiring loom, all lights,(to LGB 5v), gives constant lighting, better and brighter firebox lights, and has provisions for either an 18v or 5v smoke unit. It's a wonderful upgrade, and well worth the price. If your interested, contact Dennis @ Hillside Railways, 25746 Po Ave., Mission Viejo, CA 92691. Phone (949) 586-6292.[ Top ]
Some Shays seem to be experiencing rapid failure of the bushings that hold the wheels in place. The exact cause of the failures is up for conjecture, however a bad batch of plastic is probably part of the problem. In any event, the symptom is unmistakable, the wheels almost fall off.
My two Shays came over on the first boatload and both have many hours on them Neither shows any sign of trouble. A friend of mine put his on the track and ran it for less than an hour before ALL of the bushings began to fail or completely crumbled.
An early symptom of the failure is a wobble or looseness in a wheel. If a wheel can be turned, even a little, with respect to the other wheel on the axle, there is a problem. This will get progressively worse until the wheel comes completely loose.
Since I've never had this problem, I don't have a fix for it. However, Dave Goodson had developed a Shay Fix it Kit which is now available through Bachmann. The kit contains 8 nylon washers, 12 steel washers, 4 larger steel washers and 8 longer screws plus instructions. The kit does NOT contain replacement bushings. If you need these, make sure that you ask Bachmann for them when you order the Fix it Kit.[ Top ]
The Shay uses spring loaded ball bearings to pick up power from the wheel backs. They work well enough most of the time, but if the current load gets too high, they tend to melt down because the contacts are enclosed in plastic holders. This appears to be a special problem when the Phoenix Big Boost is used on the Shay. At low voltages, the Big Boost draws a lot of current trying to keep the sound system running at full power and several Shay owners have experienced melt down.
Hillside Railways, (949) 586-6292, has released an upgrade kit for the Shay contacts. The upgrade still uses ball bearings for contacts, but the housings are made of brass and can take the heat of high contact current. The kit provides new contact holders but reuses the motor contact tabs and the jumper tabs to the truck contacts. Hillside provides an extra set of ball bearings in case you lose some. The instruction sheet is clear and complete. The kit can be installed on both trucks in about 20 minutes with little difficulty.
After I had done the front truck, I checked it out with a Kadee contact brush. As I was testing for power pickup, I noticed that the motors seemed to run faster when the front wheels were used for pickup. I measured my power supply voltage when the motors just started to move. With the power applied to the front truck, the motors would just start to turn at 1.7 volts. When applying power to the rear unconverted truck, it took 3.9 volts to start the motors and the motor movement was much less steady. Upon conversion of the rear truck, the motors would start at 1.7 to 1.8 volts when power was applied to either truck.
The implication of the lower starting voltage is that the Hillside contacts have less resistance than the original contacts and should heat less. Because they are brass, they should be able to handle whatever heat is left even better.
If you want to convert your Shay to battery power, it is a good idea to disable the power pickups so that the loco doesn't backfeed power to the track. This can be done easily.
The original Shay power pickups are ball bearings held in plastic holders. The ball bearings are pressed against the wheel back by a small brass piston and a spring. The easiest way to disable them is to remove the springs from the backside of the holders while leaving the ball bearings and contact pistons in place. They will flop around inside the pickup housing, but without the spring, neither of them are long enough to reach the wheel and the backside contact strap at the same time.
There is a straight brass strap that goes behind the two power pickups on each side. This connects the pickups together. Also contacting this strap is a brass jumper that connects to another brass strap that goes to the top of the truck. There is also a brass tab that the motor wire is soldered to. Pull the motor tab and the jumper out of the truck. Carefully pull out the strap that goes behind the pickups. The springs will come partially out. Use tweezers to remove the springs and then put the three brass parts back in place. Then do the other side and then the other truck. Save the springs in case you want to convert the loco back. You can now feed battery power down to the motor through the original wires.
If you want to convert the Shay to a track powered command control system like DCC, you will have to do some new wiring. Track powered command control systems require that the motor and power pickup wiring is isolated from one another. Bachmann claimed at one time that they would design their locos with separate power and motor wiring, but it hasn't happened yet.
The Shay uses a spring finger contact system to connect the truck to the loco frame. The power pickups and motor connections are brought to the top of the truck on brass straps that hook over the top of the truck. This system works quite well and has low voltage drop. It also allows the truck to be easily removed from the loco for service if needed. I wanted to retain this contact system for the motor wires as well as the power pickup wires.
The contacts are pressed against spring fingers on the bottom of the truck bolster to make the connection to the engine body. From this photo, and the previous one, it can be seen that there are features available to attach a second set of contacts that could be used to feed motor power back down to the truck from the engine body.
I could have made the parts to add the extra contacts, but I elected to buy them from Bachmann instead. $7.20 bought me enough parts to do two complete locos. The bolster contacts are all the same, four are required for one loco. The truck contact straps come in a left hand and right hand version, two of each are needed. I also got the little screws to hold on the bolster contacts, four are needed for one loco.
The contact straps fit just a little too close the Hillside Railways contact kit that had been previously installed in this Shay, so I trimmed them just a little to make more clearance.
Once the contact is inserted in the truck, just unsolder the motor wire from its tab and resolder it back to the end of the new strap.
The original contact is held in place by the brass jumper strap at the bottom. Since there is nothing to hold the new contact in place, I attached it at the top with a small drop of Zap-CA CA. It would be really unfortunate if the strap should move and touch the adjacent track power contact at the bottom. This would almost certainly cause the untimely demise of a DCC decoder.
The new truck contacts connect to new bolster contacts which are simply screwed in place in the provided holes in the bolster. New motor wires are run to the new contacts and soldered.
To route the new wire to the front truck, remove the smokebox front and then remove the smoke unit. Remove the ashpan cover and then push the new wire pair down the hole in the top of the firebox along with the rest of the wires. A little fishing around will cause the new wire to head to the front. Insert the new wire pair into the truck bolster with the existing pair.
Depending on where you mount your DCC decoder will determine where the other end of the wire goes. I ran it back through the wire tunnel to the tender where a DCC decoder will eventually reside. The rear motor wires are simply run up into the tender.
I finally broke down and installed more computer power in a model Shay than ever existed in a real Shay. I installed DCC and digital sound. The systems I selected are the best currently available for the money, a Lenz LE230 DCC decoder and a Soundtraxx Sierra.
This Shay had an analog
sound system in it. I had hacked an old sound board out of an RC
Big Hauler and hung it in the Shay. I also took the speaker, which
was a surprisingly good one, from the RC Big Hauler. I determined
that this speaker sounded just as good as the best small speaker
that I had so I elected to use it.
Mounting the sound board and the decoder to the tender shell would have been both easy and difficult. The mounting part would be easy, the wiring would have been a bear. Since only two wires actually need to go to the shell (the rear headlight) attaching the boards to the shell would have resulted in a large bundle of wires going from the frame to the tender shell, an undesirable condition. I did the Climax that way and it was a pain. Not only is it difficult to wire and maintain, the continual flexing of wires as the shell was removed and installed will eventually result in broken wires and possible electrical damage if the wrong wire touches the uninsulated sound and DCC boards.
Instead, I elected to mount the boards on the back of the speaker. I attached a small piece of 0.062 styrene with foam tape to the speaker magnet and then attached the boards to the styrene with more foam tape. The boards were just short enough to clear the lead weight at the back and the SilverRidge Mining Co. oil bunker at the front. This way, all but two wires are permanently installed. The headlight wires are connected with a two pin connector so that I can remove the shell entirely for testing and maintenance. The small board in the middle holds two optoisolators used to transmit whistle and coupler clank sound triggers to the sound system from the DCC decoder. Later two more optoisolators were added to isolate the decoder motor connections from the sound system as well.
There was one complication however, the whole assembly was too tall to fit inside the stock tender shell. I can't remember how the stock coal load fitted, but with the oil bunker on top of the tender, the plastic ridges that extended down into the tender were unnecessary so I hacked them off. This allowed the boards to fit.
A standard hack for Shay sound installations is to mount the battery under the frame just in front of the rear truck. The battery won't fit well unless the wiring tunnel is removed which is no problem as the wiring can't be seen anyway. The battery can be seen, but since it is black and nondescript, it isn't visually obtrusive. The bright red and white lettering faces downward so it cannot be seen.
I wired the system two different ways. The first way was a little simpler, but it couldn't keep the battery charged. The second way keeps the battery charged but is slightly more complicated.
Running without any charge source at all, the Sierra sound system will discharge its battery in about 45 minutes. When the system is wired with connections 7 and 8 connected to an average motor, the battery will get some charge and the system will run for maybe 2 hours. Running from a DCC decoder which outputs PWM and charging from the motor as shown in the first schematic, the battery will last maybe 4 hours or so.
However, even this didn't satisfy me so I rearranged the wiring again so that the battery is continuously charged from the 9 volt regulator on the Shay flicker board and the battery will NEVER run down when run from DCC on the track. With Aristo PWC on the track the battery will get net charge as long as the engine is moving, even very slowly. With DCC on the track and the battery completely flattened by running with the flicker board turned off, the system will start to run again immediately when the flicker board is activated and it begins to charge the battery. With DCC, the battery will be trickle charged as long as the engine sits on DCC energized track, running or not.
The first method that I chose is very simple wiring scheme. Soundtraxx recommends a different approach in their Technical Note #7. They recommend not using the battery and running the sound system from DCC track power. Since I wanted this engine to run on analog track power as well as DCC (my DCC conversion is going slowly and analog conversion is important to me for the interim) I elected to retain the battery and allow it to charge from the PWM pulses generated by the DCC decoder. The disadvantage of this approach is that optoisolators are necessary to isolate the DCC decoder function outputs from the sound triggers. Installing optoisolators is no big deal, see my Sound Tips page for details.
Even though the Sierra has its own flicker circuits that could drive firebox lights, the Sierra lighting circuits draws power from its battery so I elected to minimize the load on the Sierra's battery by retaining the Bachmann flicker board. I did hook the flicker board to track power through a switch so that I could disconnect it from the track during decoder programming.
I also replaced the stock Bachmann smoke element with an LGB 24 volt element. At my track voltage of 22 volts, the LGB element really cooked, quite literally. It smoked much too strongly. Adding a resistor in series with the smoke element decreased its dissipation to about 1.5 watts. This is the same dissipation as the 5 volt elements which smoke fine and also seem to have a very long life and are tolerant to running dry.
The Sierra is hooked up only to the motor leads of the Lenz DCC decoder and through optoisolators for function control. This is the safest approach and the least likely to cause any damage to the DCC decoder or to the Sierra. The Sierra then senses motor voltage and can operate its voltage controlled effects based on engine speed. However, there was a problem. The Sierra was being fooled by something coming out of the decoder. It would only play its starting or stopping effects when the DCC power was applied or removed from the track. Even though the chuff (wired to the Bachmann sound switch contacts) and bell worked fine, the automatic whistle signals did not.
I guessed that there had to be switching transients leaking out the decoder that were confusing the Sierra so I added a 0.1 uF capacitor across the Sierra's input (the decoder's output) and the effect changed. The forward startup (two toots) and the stopping sounds (hiss and one toot) worked OK, but the reverse signal played the forward signal instead. I consulted with Soundtraxx and they recommended adjusting the auto-exhaust startup voltage. While this did have some effect, it didn't fix the problem.
I found by experiment that a more substantial RC filter was necessary to clean off the switching transients that were confusing the Sierra. I settled on a 10uF NON POLARIZED capacitor and a 22 ohm 5 watt resistor as the filter. Smaller capacitors (1 uF) did not have sufficient filtering effect, and smaller series resistors allowed too much ripple current to flow to the capacitor which beat up on both on the resistor and the decoder.
With a fully charged battery, the Sierra draws about 60 mA at idle (above 9 volts which is necessary to wake up the unit), about 200 mA fast chuffing and up to 500 mA fast chuffing with the whistle blowing so there can be substantial dissipation in the resistor. Also, when charging the battery, the unit requires 10 volts and draws an input current of about 250 mA without the chuffs or whistle. At a 400 mA typical load (200 mA to run the system while chuffing and 200 mA to charge the battery), the resistor drops about 9 volts but still allows the Sierra to try to charge the battery from the DCC decoder motor pulses. It is important to charge the battery at the maximum rate possible as it will charge only when the motor pulses are actually on.
When the whistle is blowing, the resistor can get slightly overloaded but since the whistle doesn't last too long, this isn't a problem. The resistor also removes significant dissipation from the internal regulator in the Sierra which would get rather hot otherwise. Even with this filter, some adjustment of the auto-exhaust start voltage may be required.
There is dark side to using an external resistor. When the whistle blows, the voltage drop in the resistor increases and the voltage delivered to the Sierra decreases. When the whistle signal finishes, the current goes down, the voltage applied to the Sierra increases and the Sierra thinks that it got another whistle trigger and blows the whistle again. The thing turns into an oscillator, continually retriggering itself. You will need to set the whistle sensitivity and filter rate such that the automatic grade crossing whistle NEVER blows or it will NEVER STOP blowing. Try a sensitivity value of 10 and a filter rate of 1. That should kill it for good. If you really want a grade crossing signal, wire a decoder function to trigger the whistle through an optoisolator so that it will blow ONLY when you want it to. See my Sound Tips page for details on using an optoisolator.
Note that if you do trigger the whistle with a decoder function, you will get only the grade crossing signal unless you program the remotely controlled whistle mode where you have to blow all the whistles yourself, the automatic whistle signals are disabled. The Westside Shay version of the Sierra does not have particularly good remotely controlled short whistle signal control, actually it is pretty poor. You'll be more pleased with the automatic whistle signals.
This method worked pretty well, but after extended low speed running, 4 hours or more, the battery would still become discharged and the sound system would freak out. The symptom of a discharged battery is continual popping and whistle blowing as the system shuts down and resets. This doesn't hurt the system, but it sounds terrible.
To fix the battery charging problem, I elected to rearrange the wiring. Instead of trying to charge the battery from the motor circuits through the Sierra, the battery is charged by an on board charger derived from the 9 volt regulator on the Shay flicker board. A diode and a resistor are added in series between the regulator and the battery. The diode prevents the battery from discharging back into the regulator when there is no track power. The resistor limits the charging current so that the battery will not be cooked and the regulator will not be overloaded. A 10 ohm resistor allows the system to run from the regulator even if the battery is flat. After the sound system takes it share, there is still enough current left over to charge the battery at a low rate. If the sound system is turned off with the battery flat, the charge current is limited to about 200 mA which is the rating of the battery. When the battery becomes charged and its voltage increases, the charge current decreases to a 25 mA trickle which the battery can handle continuously. Note that the battery is always hooked up the charger circuit.
The connections on the flicker board to pick off the +9 volts and ground are not marked. +9 volts is most easily found on the center pin of the regulator. Ground is found on one lead of R2, a 1.5K resistor. On my unit, R2 was stuffed on the board such that the lead on top was the ground lead. Its the one nearest the center of the board. The resistor on your unit might be stuffed differently so you need to check to make sure that you are really using the ground lead.
Soundtraxx provides a circuit in their Technical Note #7 which shows that the Sierra can be connected to the track though a power supply circuit and still be connected to a motor on a DCC decoder. Maybe this works, but I have never trusted these "virtual ground" type connections. I elected to optoisolate the motor connections to the Sierra as shown in Technical Note #6 when the Sierra is connected to an Aristo 5490 mini-receiver. This approach requires two more optoisolators and three resistors, but it works very well and completely isolates the sound system from the DCC decoder. Optoisolators are cheap and reliable.
Depending on the polarity of the motor drive signal, one of the two optoisolators is activated and either pin 7 or pin 8 of the Sierra is pulled up. The Sierra can use this kind of signal to determine the motor voltage (based on pulse width) and polarity to operate its voltage controlled effects. This circuit gave me no troubles like I had with the direct connection and I recommend using it even if it doesn't seem to be absolutely necessary. It is cleaner and safer.
I finally had a wheel loosen up on one of the Shays. To tighten it requires that the brake beam and bearing assemblies be removed. This is not difficult, but a lot of screws have to be removed to tighten one lousy wheel mounting screw.
truck needs to be removed from the engine. On this older truck, the
two long screws on the bottom cover (the ones in the middle at each
end) need to be removed. On newer trucks, these are under the
bottom cover. Then two short screws need to be removed from way
down in those square black holes at both sides near the center.
Once these screws are removed the truck can simply be lifted off
The entire brake beam and bearing assembly must be removed in one piece. It slides off (with some difficulty) upward. To remove it, the drive shaft has to come off. There are four screws that hold on the shaft. When the screws are removed, the entire shaft assembly will come off. The gear covers will simply pull off. There is also a small screw on each side at the lower center of the sideframe which must be removed. One of them can barely be seen in the upper right of this photo.
There are four more screws, two on each end of the brick that must be removed. To get to one of them on the end with the coupler mount, the mount must be removed also. The brake beams are still held in place by four pins, two at each end of the truck. The ends of the brake beams can be gently pried away from the brick to release the pins. Then the whole brake beam and bearing assembly can be worked upward and off of the truck. This exposes the wheel mounting screws that get loose and infamous bushings that crumble.
At this point, the wheels can be removed and the brushes either serviced or removed during a battery R/C conversion. You might also want to check the nuts that hold the gear plates against the motor. They tend to get loose.
Reassembly is done in the reverse order.