BUFFALO CREEK #43
ALCO HH660
Updates 2022
by WNYRHS
March 2022
April 2022
At our next work session, the weather covers on the radiators will need to be removed and 205 gallons of water, "borrowed" from ArtCraft Toy Trains (Hamburg Depot), will be added to the cooling system. Fresh diesel fuel with "Diesel Kleen" additive will be added to the fuel tank and the locomotive will be ready to start. It would be great if you could become a Society Member and join in the fun! |
May 2022
As the cooling system filled, Rick "barred" the engine over to release trapped air in the water passageways. In less than an hour, the water gauge in the cab showed 3/4's full in the expansion tank, and the water was turned off. With the engine being barred over and five gallons of fresh diesel fuel, the engine was ready to start. |
He unlocked the control stand, closed the battery switch, and started the fuel pump. When 35psi showed on the fuel pump gauge, he hit the started button. "Ca-chunk, ca-chunk, ca-chunk, ca-chunk, the engine coughed a few times, revved up and died. After a few tries with the same result, he knew he needed someone to "stick a screwdriver in the carburetor," Ha! This phrase goes way back to the days when you stuck a screwdriver into your 2 or 4 barrel carburetor car to keep the choke open. |
With the locomotive running again, we need to continue the repainting project started last year. Sander pipes, hangers and nozzles need to be fabricated. There is plenty of work for anyone, no matter what your skills are. We have all the tools and supplies, all we need is a little of your time. Please contact us at the eMail address below if you want to become part of the team and become a WNYRHS member. |
Rick was back by himself, at the Hamburg work site on May 9th. #43 started right up and was run for almost an hour and half. While the engine idled, Rick topped of the cooling system one more time and sprayed "Round-Up" on all the vegetation around the engine. |
Rick returned on May 23rd, checked the oil and water fluid levels and started the engine again. After running the air compressor for ten minutes, he was ready to make the first moves in 2022. With a little brake shoe squeal, #43 was off and moving again. For an hour and fifteen minutes, he made the 80 foot move up and down the siding. |
Below is a brief summary of the work Rick Burns completed on #43 over the summer and fall by himself. |
June 2022
6/6/22 - Ran for 1.2 hrs. Made multiple forward and reverse moves. Found a small leak at on the water pump shaft. After tightening the packing ring, the leak stopped. 6/14/2022 - Ran for 1.3 hrs. Made multiple forward and reverse moves. Aux. hour meter was not working in electrical cabinet. Moved lever on fuel pump strainer. 6/23/2022 - Ran for 1.2 hrs. Made a few forward and reverse moves. Repositioned Aux. meter from inside electrical cabinet to under main meter on cab control stand. |
July 2022
7/1/2022 - Ran for 1.1 hrs. Made multiple forward and reverse moves. Installed Aux meter using news wires. (#60 and #65). Added one 64 ounce bottle of "Diesel Kleen" to fuel tank. 7/13/2022 - Ran for .7 hrs. Made multiple forward and reverse moves. Installed Aux meter using news wires. (#60 and #65). Added one 64 ounce bottle of "Diesel Kleen" to fuel tank. 7/13/2022 - Ran .7 hrs. Made a few forward and reverse moves. Looked for possible damage from vandals reported on 7/10/22, nothing was damaged. Cleaned one fuel strainer basket for fuel pump. 7/22/2022 - Ran 1.3 hrs. Made multiple forward and reverse moves. 7/26/2022 - Ran 1 hr. Made multiple forward and reverse moves. |
August 2022
8/19/2022 - Ran 0.4 hrs. Made multiple forward and reverse moves. 8/24/2022 - Ran 1 hr. Made multiple forward and reverse moves. Weed wacked along track and around locomotive. 8/31/2022 - Ran 1.1 hrs. Made multiple forward and reverse moves. |
September 2022
9/9/2022 - Ran 1.1 hrs. Made multiple forward and reverse moves. Added another 64ozs of "Diesel Clean" to fuel tank. 9/23/2022 - Ran 1.3 hrs. Made multiple forward and reverse moves. Forward headlight not operating. Removed and cleaned fuse, headlight now working. |
October 2022
10/11/2022 - Ran 1.3 hrs. Drained cooling system and reinstalled weather covers. Below 32' temperatures expected this weekend. Voltage check on batteries showing 118.1 volts. 10/27/2022 - Cranked engine to remove all residual water. (engine started and was quickly shut down) |
At the end of the season, #43 was run for 60.35 hours, used 76.37 gallons of diesel fuel for a total cost of $434.10. Thank you Rick for taking care of this historic piece of equipment! |
The WNYRHS greatly appreiciates all the generous donations to this project to date. However, we could still use your help! All Donations are Tax-Deductable! If you would like to mail a donation, send it to: |
or Click the PayPal Button to make a Secure Electronic Donation. THANK YOU! |
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